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Full-scale embankment failure test under simulated train loading

Lehtonen, Ville; Länsivaara, Tim; Mansikkamäki, Juho; Meehan, Chris (2015)

 
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Full_scale_embankment_failure_test_under_simulated_train_loading.pdf (1.201Mt)
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Lehtonen, Ville
Länsivaara, Tim
Mansikkamäki, Juho
Meehan, Chris
2015

Geotechnique
This publication is copyrighted. You may download, display and print it for Your own personal use. Commercial use is prohibited.
doi:10.1680/jgeot.14.P.100
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Julkaisun pysyvä osoite on
https://urn.fi/URN:NBN:fi:tty-201701091032

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Peer reviewed
Tiivistelmä
A full-scale embankment failure experiment was conducted in 2009 in Perniö, Finland. A small, extensively instrumented railway embankment on a soft clay foundation was brought to failure by loading over a period of 30 h. Instrumentation consisted of over 300 different measurement points, including 37 piezometers and nine automatically monitored inclinometer tubes. The relatively rapid loading simulated a heavy train coming to a standstill on the embankment. The primary purpose of the experiment was to gather field data of a failure caused by a rapidly applied load, with an emphasis on the pore pressure response in the clay foundation layer. The test was also used to assess the suitability of various instruments for real-time stability monitoring. The embankment failure was an asymmetric bearing capacity mechanism that is hypothesised to have been triggered by an undrained creep rupture.During the last 2 h of the experiment, pore pressure and displacements increased at an accelerating rate while the external load was kept constant. The time-dependency of the pore pressure and displacement responses was a key factor in the experiment. With regards to monitoring of similar in-service train<br/>embankments, proper placement of instruments according to predicted failure mechanisms was found to be important.
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Kalevantie 5
PL 617
33014 Tampereen yliopisto
oa[@]tuni.fi | Tietosuoja | Saavutettavuusseloste